10-13-2020, 04:14 PM
(10-11-2020, 03:26 PM)cliffyk Wrote: As we are clamping a sphere, the perimeter of the inverse conical nose of the OEM set screws will want to do one or two, or both, of two bad things; a) they will dig into the sphere and make irreparable divots that will become the new favourite seating/setting positon for the sphere and screws, or b) they will cause the sphere to rotate along the screw nose's path as the screw is tightened screwing up (no pun intended) up any positioning of the platen just accomplished.
I also put a dab of high pressure grease on the screw's new ball nose to minimise any tendency of he screw's nose to rotate the sphere.
That's what I originally thought but actually the set screws impinge on a split cylinder that is between the sphere and the screws. The split is between the two set screws so in theory, the sleeve is pushed in and squeezes the ball.
I did adjust z bearings and can say that stepper motor stalled when it tried to drive the arm off the top of the ball screw. I had to pull up on the arm while simultaneously hitting the up button repeatedly. Not a graceful process. The rods upon which the bearing ride seemed to be narrower at the very top. The rest of the travel up the mast didn't cause any audible lost steps. It needed quite a bit of adjustment to be able to reinsert the z stage. From all the things I've seen on forum, I'd suggest that every new owner just make this adjustment before getting started.
Of course that didn't fix my problem. Yesterday I made another run with standard exposure conditions with a 100 micron sheet for zero and the slant persists and the back is a bit thicker than the front. I print a small open rectangle inside a larger rectangle and have had the smaller rectangle separate from from the FEP about 2/3 of the way through the print. Today I increased the base layers exposure to 75 s from 60 seconds and other layers to 10 s from 8 second. Zeroed off a 100 micron sheet as before. The rectangle pictured is the result. The thick end is about 0.7mm thicker than the thin end. The step backwards results in a 3-4 degree slope. The Z mast tilt backwards maybe 0.1 degree (tilt meter read 0.1 degree off normal when base has zero tilt but meter is supposedly only accurate to +/- 0.3 degree) so it's not the cause of the problem.
I was going to make another run with a zero on 180 micron sheet but during tightening of the front set screw, the thread in the aluminum housing was stripped. I should admit that I replaced the socket screws with a hex head since I thought maybe the original screws might be limited in the amount of force they could apply to the sleeve since it looked like it's shoulder might bottom out on the recess. So I'm out of commission for awhile until I replace this part. Maybe the problem I'm seeing is related to something on that head or the ball lock system, so maybe a new head might give superior results.